#226
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that car is so bad ass but she look rough when we gonna see some beauty in this beast!
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YEAH ITS GOT A HEMI |
#227
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Well, since paint doesn't make it go faster, it'll be the last thing on the car. I do want to get it painted this year if possible, I'm tempted to do it myself here at the house.
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#228
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whaaatttt??? paint doesnt make it faster? ive been lied to! lol just kidding i see what you mean dont be scared paint it one nice evening outside lol
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YEAH ITS GOT A HEMI |
#229
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put it in flat black primer and roll it.
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NO_H2O 72 1302 Smack Black GL 73 Bus (2L CIS Powered) 66 Beetle, 73 Standard Beetle 72 Pinzgauer 710M Volksport Kafer Gruppe |
#230
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Got her running again with a couple updates. Updated tuner studio and went back to an earlier tune. Also swapped out the dead LC-1 for a new one, and changed the O2 sensor just in case. I installed a new ground on the oil tank so maybe the oil temp gauge would read correctly, and rerouted the 1-2 cylinder head temp wire for the same reason. Once she was running I reset the mechanical timing which solved a lot of the starting problems.
I took her for a short spin down the hill and had a cloud following me back up. The sand seal didn't do anything for the oil leak and it just poured oil as soon as I hit 2-4psi boost. These oil leaks are killing me :P |
#231
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Do you have a good size breather system?
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NO_H2O 72 1302 Smack Black GL 73 Bus (2L CIS Powered) 66 Beetle, 73 Standard Beetle 72 Pinzgauer 710M Volksport Kafer Gruppe |
#232
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I'm running 1/2" lines on each valve cover and the oil filler neck. There's also a 1" vent/filter on the top of the oil tank as well.
I know the dry sump pump isn't strong enough to pull a vacuum but it seems like there is excessive crank case pressure to me. I thought it might be that the rings haven't seated yet as there is only 2 hours of dyno time on this motor, but it should be dry from the get go. |
#233
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Quote:
And still, just a few psi boost should be possible without leaking on seals that badly.. Keep the spirit! even though this is frustrating as h*ll. |
#234
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Any updates?
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Everyone told me its not a good idea to daily drive an aircooled bug. I agree, if the engine has a distributor and you use cheap engine parts... OR you have an early car without the decklid vents or you neglect to add an oil cooler with fan... |
#235
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weather and side jobs have kept me from working on the bug unfortunately, but hopefully that will turn around in the next week or so. I have a little bit of cash and I'd like to get the car back to the dyno.
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#236
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This is a seriously cool car!
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#237
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I finally had some good luck with Lucy. I swapped out the BMD pulley kit for a different sand seal setup and found that I hadn't machined the back face of the crank pulley enough so it cut the sand seal rendering it useless. No wonder it was pissing oil! New seal, new pulley, and everything seems dry. Underneath the motor, the oil relief plug was leaking under high oil pressure (anything over 30psi really) so I pulled it and changed the compression washer. After warming up the motor I loaded the engine up using the brakes (don't do this kids) to build some boost and managed 12 psi at about 6000 rpm. Shut everything down and checked for leaks, only to find that the crank was dry! The relief plug has a very small drip (one or two a minute) under high rpms but other wise everything else is dry.
During the first warmup I had some crazy lean spikes that would kill the motor after cold start. I've been slowly working on my cold start enrichment to perfect it and getting a little closer every day. I've also been working on the fuel map to work out super lean areas when cracking the throttle. Slowly but surely she's coming along, and another dyno day is in the future. I have a NASA track day weekend coming up at the end of August at Thunderhill which I would love to take the bug to but I might run out of time. Video forth coming... |
#238
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Here's the video as promised. She's still running a bit rough with a mean lean spike whenever I touch the gas from idle. Seems better above 3000 rpms but still leans out a bit. The throttle response is very slow too and I'm trying to work that out. Going to schedule a dyno day next week and hopefully she'll be ready ready in August!
http://www.youtube.com/watch?v=SC0n2zEMikU |
#239
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sounds really mean man... nice work hope to see it on the track With some video
Chris.
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74 Std. GL 08 Vw rabbit 18 WR250R 07 Chevy 3500 Dually |
#240
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You will get it ironed out. Then we need some in-car video.
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NO_H2O 72 1302 Smack Black GL 73 Bus (2L CIS Powered) 66 Beetle, 73 Standard Beetle 72 Pinzgauer 710M Volksport Kafer Gruppe |
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